I have currently got the somewhat scruffy Type 70 Steyr Puch Invalid Carriage up for sale. I made no great efforts on this to get the ball rolling. Just a scrub, and wash off. Fitted the doors. Its on Car and Crashit classified.
The thought was as and when pockets of time came available I can tidy it a bit further as the ad runs. So the remains of the tow hitch have been removed. The rear lights, a very good pair of the correct early fitments, as this example was withdrawn before all the lights were changed, were fitted. The correct boot stay was located in the parts and added.
Andrew helped me attempt to start the engine. This proved problematic. The electricity was only reaching the solenoid for the starter. Using a long feed cable I checked the sections of wire beyond. There were numerous poor connections, resistances and faults. I therefore decided to use a complete spare primary wiring loom we had in second hand spares. This was cleaned up on the bench. Then it was mounted loosely. It immediately became apparent that there was a wiring discrepancy. Logic bought to bare said the car on was wrong, as the live feed to the ignition switch was the wrong side of the Solenoid, meaning it would be impossible to switch on. That thought was put behind my ear, as it were.
So with the wiring now of a known conductivity throughout, we tried again. Nix. Now the ignition switch was getting no live feed. I swapped it for a serviced one, just because. Then looked for the big brown live wire that should provide the current. It left with, arrived without, gaining a white tag on the way. The joint was traced back to the fuse holder. The live feed clearly should have powered the one contact, with the brown/white wire next to it going on to the ignition, The lights being on the other side of the fuse. What I had, was no fuse, and the brown wire on one side, the brown and white on the other, isolated, and another wire, live. Ear lodged wiring fault, removed from ear. So it was hot wired. Turning the fusebox back to the correct layout, and we had ignition switch power. From then on the starter was very happy to spin, much more so then previously, when supply was put onto the feed wire from the old solenoid and wiring loom. Proof, if you need it, of the loss to resistance time corroded connections offer.
A current check on the coil, and to the points, revealed continuity, but the dissy needed a good spring clean. I do not know if cobweb is a conductor, but decided not to find out. All looked good for a fire up. So off with the air filter, it does have one of the flap control springs on it, so a bit of fiddling to retain adjustments. Bit of fuel down the carb and the engine fired up pretty readily. It sounded very quiet, and smooth. Bodes well, as these units out of tune, or worn, can be lumpy and rather laud.
So to the fuel supply. There wasn't any. The fuel tank was pulled and contained some of the bitterest tasting petrol I have had in my mouth. The entire pipe was gummed despite repeated attempts to clear it. The gunk reformed a barrier. So a bench clean up. All pipes sorted, it was back together. Still no fuel coming out for the carb. Lifting the tank I could feed fuel direct into the carb. In this way the engine ran. But we were about to loose battery power, and it was clear that the pump needs a rebuild. Maybe the carb will need a clean up too. But done the machine can have its drive system tested. The engine sounds like a very good unit.
Its still on Carlos Fandango wheels. I will source a set of proper wheels for it shortly, and tidy up the wheel arches. If we get the car running, it then becomes an issue to get the brakes working, as the car will be drivable. I think at that point I will be looking at breaking up the duffed Mk12, so as to make its front panel available for the Type 70. For with that nose modified to fit, and the car driving, it passes to being a more valuable vehicle and will require a new advert at a higher price. Indeed, but for having so many projects I would do it up to a good standard. Its an easy restoration.
Good progress made, then.